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Program-rific


We tried to program our robot to accelerate from 0.2 to 0.8 as it jerked for small movements.

Moreover, we also moved our gears up the robot for efficiency and so that it works better.

This is our result.

We also switched the gears because they weren’t meshing properly.

Today we had a fun mix of programming and building, and this mostly came to fixing errors.

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